Omega Owners Forum

Omega Help Area => Omega General Help => Topic started by: elitedave on 12 April 2013, 15:00:17

Title: Suspected head gasket failed 3l v6
Post by: elitedave on 12 April 2013, 15:00:17
Re looks like I'm stuffed Thead and seized tension pulley and aux belt and leaking radiator

Just got it all back together after putting in new radiator pulley and belt

Start and seems to be running ok on all cylinders and don't seem to be running too bad
temp seems stable to
But coolest is pussing out under car and trickerling off sump

It not coming from anywhere near what's been touch ie up frount by radiator

And steam from under back of plenuim thing
Hbv is fine checked so is heater hoses only done heat matrix few weeks back

Is it worth look anywhere else for a leak or do you guys thing it is defiantly the head gasket


As if it a top end rebuild I'd beyond me and I'm running out of cash fast




So I'm guessing it the head gasket
Title: Re: Suspected head gasket failed 3l v6
Post by: amba on 12 April 2013, 15:22:20
Take the plenum and inlet manifold off followed by the lower sandwich plate to have a really good look at oil cooler plate/thermostat and coolant bridge area.

They are all very strong possible areas that can leak and give the very symptoms you are describing
Title: Re: Suspected head gasket failed 3l v6
Post by: elitedave on 12 April 2013, 15:27:13
Could a overhead from a failed aux belt cause that
Title: Re: Suspected head gasket failed 3l v6
Post by: tunnie on 12 April 2013, 15:29:40
Worth checking the oil cooler plate & coolant bridge area, not unknown for one of the pipes at the back to split and pish coolant all over the place.
Title: Re: Suspected head gasket failed 3l v6
Post by: zirk on 12 April 2013, 15:39:03
Could a overhead from a failed aux belt cause that

Was the Car / Engine being used after the Aux Belt problem, if so, how long for?
Title: Re: Suspected head gasket failed 3l v6
Post by: elitedave on 12 April 2013, 15:54:00
Was on duke charge way when it went had to drive to ther was a turn off few hundred yards

Where radiator was pissing out all over electrics and it was dar I cout not see belt and wrongly asuned power steering outage was due to water from lradiaitor leak

So re filled when cooled and drive one mile after that it was towed
Title: Re: Suspected head gasket failed 3l v6
Post by: JayMV6 on 12 April 2013, 15:58:47
Could it be just excess water thats sat in between the heads from when you lost water. when u first broke down was engine covered in water?x
Title: Re: Suspected head gasket failed 3l v6
Post by: TheBoy on 12 April 2013, 16:01:48
Plenum off, along with inlets, so you can see right into the V.

Join or block the 2 pipes that you removed from throttle body to remove plenum.

Pressurise the coolant to about 8PSI (blowing hard into one of the pipes above will work) - coolant leak will be obvious.
Title: Re: Suspected head gasket failed 3l v6
Post by: elitedave on 12 April 2013, 16:30:21
car was at my mothers place where i had it towed to from essex

i justed brimed header tank and drove home to my place couple of miles away temp stayed in right rang and lost about 3 liters on way took it back too mine to get tools back here and car

but its well down on power

im well not happy as aint got money foer  another car and are in a mess for transport now

Title: Re: Suspected head gasket failed 3l v6
Post by: symes on 12 April 2013, 17:42:02
if you down on power and do you have lots of exhaust smoke-then you likely hhave killed h/gaskets-is oil on dipstick coffee colored ??? When i did my old engine it was smoking like a ******* and no power/oil filler full of white gunge and dipstick was saying I had 3/4 level coffee :'( :'( :'( sorry mate reckon you done h/gaskets IMHO
Title: Re: Suspected head gasket failed 3l v6
Post by: TheBoy on 12 April 2013, 17:50:04
Extreme overheating is a worry, but do tests I suggested to locate leak.

If HG has failed due to overheat, inspect heads very closely
Title: Re: Suspected head gasket failed 3l v6
Post by: zirk on 12 April 2013, 17:54:15
Was on duke charge way when it went had to drive to ther was a turn off few hundred yards

Where radiator was pissing out all over electrics and it was dar I cout not see belt and wrongly asuned power steering outage was due to water from lradiaitor leak

So re filled when cooled and drive one mile after that it was towed

Hmm,Im 50 50 on this one,it doesn't take much to do a HG on the V6 without the Water Pump running, I know from experience when the Ex killed off one of my Plods after driving it for 5 mins when the water pump pulley threw the Aux belt!

Does it sound completely normal when you turn the engine on the starter?.

Im up the road from you if you want a second opinion, might not be the right one, but 2 heads are better than one and all that. ;)   
Title: Re: Suspected head gasket failed 3l v6
Post by: symes on 12 April 2013, 18:28:21
Lets face it people-any engine especially v6 mig will do H/G's in if no coolant-no brainer really-so but its true-I had that a few weeks ago and was quicker/cheaper to change engine on mine(243000 miles) anyway
Title: Re: Suspected head gasket failed 3l v6
Post by: elitedave on 12 April 2013, 22:12:24
Was on duke charge way when it went had to drive to ther was a turn off few hundred yards

Where radiator was pissing out all over electrics and it was dar I cout not see belt and wrongly asuned power steering outage was due to water from lradiaitor leak

So re filled when cooled and drive one mile after that it was towed

Hmm,Im 50 50 on this one,it doesn't take much to do a HG on the V6 without the Water Pump running, I know from experience when the Ex killed off one of my Plods after driving it for 5 mins when the water pump pulley threw the Aux belt!

Does it sound completely normal when you turn the engine on the starter?.

Im up the road from you if you want a second opinion, might not be the right one, but 2 heads are better than one and all that. ;)

its kind of you m8 but it i luton now not Harlow would have loved a second opinion


girlfriend is in Harlow i live in luton m8
the belt pop`ed on the a414 just before  east wick roundabout and want really any where to stop but east wick turn off it was only two roundabout up that i drove after refilling to the 

was going to Harlow station roundabout as she lives just of the station roundabout

 TheFatShadow tomorrow im going to pull it all off and look under there at oil cooler and that
thing there aint no smoke there was at first but it wa pissing down thing was just warter in end of pipe after a min no smoke but now thers no smoke to speek of

i think it probably is head but there a hell of alot of coolant pissing out form out side rather than inside of engine

but im going to try anyway with crossed fingers as i would like to keep for now if i could

it got to be worth a try if its not leaking there

and it head im going to cut my losss and move on
and scrap it as i cant break it as no where to keep it off road and break it

unless any one wants to make an offer for spares or repair



back arches were due to be done as starting to rust but its only got 105k on it iv had it since 40k suspensions been done done heat matrix just had new front wishbones for all German parts 4 mouths ago

just had new back box and two new mid boxs and pipes
one of the guys of the forum done my water pump and cam belt kit not that long ago for me

and now a new radiator and aux belt and pulley

crank sensor been done since i had and i done the abs ecu already

only thing wrougn with other than this was driver heated seat element dead couple of l bulbs need changing back arches now need doing and a small rust bubble on bottom of back door
and i was going to spray front splitter as girlfriend court it on a curb




Title: Re: Suspected head gasket failed 3l v6
Post by: dbug on 13 April 2013, 16:19:26
With plenum and inlet manifold off, look carefully around coolant bridge.  If its p*ssing out likely to be rubber hose from coolant bridge to HBV (the "curly" one).  Flex it and look for holes around where its clamped to coolant bridge.  Also check its not leaking from the coolant bridge seals, although wouldn't expect it to p*ss out fron here unless they are completely gone.
Also check oil cooler plate and thermostat housing while stripped.
Title: Re: Suspected head gasket failed 3l v6
Post by: dbdb on 13 April 2013, 16:28:59
Water boiling in the cooling system would likely blow a hose or some connection or plug  and the lack of steam from your exhaust is encouraging.  The loss of power though is not.  If the head gaskets gone its gone so run it keeping the water topped up while you try and identify the leak and hope it hasn't. 
Title: Re: Suspected head gasket failed 3l v6
Post by: elitedave on 13 April 2013, 17:51:28
i was going to have a look today but iv just been up a and e

its not my bloody week the dog 8 week old puppy run at my feet when i had a hot coffee iv gone over on me ankle

tort id busted it took some Codine and rum woke up and it swollen up like a balloon

back now after 4 xrays with more pain pills not broken just bad sprain and ripped ligament
 
Title: Re: Suspected head gasket failed 3l v6
Post by: symes on 13 April 2013, 18:09:06
i was going to have a look today but iv just been up a and e

its not my bloody week the dog 8 week old puppy run at my feet when i had a hot coffee iv gone over on me ankle

tort id busted it took some Codine and rum woke up and it swollen up like a balloon

back now after 4 xrays with more pain pills not broken just bad sprain and ripped ligament
 
sorry mate-but could have been worse!  get well soon mate-hope you have speedy recovery :y :y :y
Title: Re: Suspected head gasket failed 3l v6
Post by: elitedave on 14 April 2013, 01:28:22
thanks m8

just looked at todays weather gong to be sunny and about 16 degrees 

just my luck could have done with a few hours out on harley to get away from stress

not going to happen with a ripped up foot grrr
Title: Re: Suspected head gasket failed 3l v6
Post by: Gaffers on 14 April 2013, 08:08:41
[car talk off]

Sounds like you did your ATFL (Anterior Tib-Fib Ligament) which is a very painful injury.  I'm sure you were told in A&E about RICE, Rest Ice Compression Elevation.  So no working on cars or walking very much for the next few days.

Try and pressure your doc for some physiotherapy.  It hurts like hell but it will help your rehabilitate better.  If you can, buy a wobble board and do circular exercises with it.  Damage to the ligaments means you loose that joint memory which means you will likely go over on it again, and it will hurt like a bastard.  When I did mine I took it to work and put it under the desk doing my exercise all day.  I also used an ankle support like this one:

http://www.physioroom.com/product/Aircast_Sport_Stirrup_Ankle_Brace/2030/35946.html (http://www.physioroom.com/product/Aircast_Sport_Stirrup_Ankle_Brace/2030/35946.html)

Not cheap but well worth it, you could even try and get one through your doc.

Wobble board:

http://www.amazon.co.uk/dp/B0057EQHA6/?tag=hydra0b-21&hvadid=9550951269&ref=asc_df_B0057EQHA6 (http://www.amazon.co.uk/dp/B0057EQHA6/?tag=hydra0b-21&hvadid=9550951269&ref=asc_df_B0057EQHA6)

Exercises, a bit cheesy but what they say and do is correct:

http://www.youtube.com/watch?v=_EmdOu_GOK8 (http://www.youtube.com/watch?v=_EmdOu_GOK8)

Good luck! (From a fellow ankle sufferer)

[Back to talking about cars]
Title: Re: Suspected head gasket failed 3l v6
Post by: elitedave on 14 April 2013, 09:45:13
[car talk off]

Sounds like you did your ATFL (Anterior Tib-Fib Ligament) which is a very painful injury.  I'm sure you were told in A&E about RICE, Rest Ice Compression Elevation.  So no working on cars or walking very much for the next few days.

Try and pressure your doc for some physiotherapy.  It hurts like hell but it will help your rehabilitate better.  If you can, buy a wobble board and do circular exercises with it.  Damage to the ligaments means you loose that joint memory which means you will likely go over on it again, and it will hurt like a bastard.  When I did mine I took it to work and put it under the desk doing my exercise all day.  I also used an ankle support like this one:

http://www.physioroom.com/product/Aircast_Sport_Stirrup_Ankle_Brace/2030/35946.html (http://www.physioroom.com/product/Aircast_Sport_Stirrup_Ankle_Brace/2030/35946.html)

Not cheap but well worth it, you could even try and get one through your doc.

Wobble board:

http://www.amazon.co.uk/dp/B0057EQHA6/?tag=hydra0b-21&hvadid=9550951269&ref=asc_df_B0057EQHA6 (http://www.amazon.co.uk/dp/B0057EQHA6/?tag=hydra0b-21&hvadid=9550951269&ref=asc_df_B0057EQHA6)

Exercises, a bit cheesy but what they say and do is correct:

http://www.youtube.com/watch?v=_EmdOu_GOK8 (http://www.youtube.com/watch?v=_EmdOu_GOK8)

Good luck! (From a fellow ankle sufferer)

[Back to talking about cars]

thank m8
dose sound like your right just goggled the ATFL and that exactly where swelling is its don down a fair bit this morning

funny you say about going over on it again iv feel on both ankles ie rolling over on like that a few time but never this bad

if got rather doggy balance as my hips are out of line twisted due to scoliosis kills me working on car any way poped a disk a l4-l5

iv got problems with thoracic and cervical spine too a a fair bit of nerve pain as well
Title: Re: Suspected head gasket failed 3l v6
Post by: Gaffers on 14 April 2013, 12:37:12
Sounds like you definitely need physio.  If you have scoliosis then your whole biomechanics need looking at to avoid future problems.  You may need shoe implants or something more drastic.  In the meantime look after your ankle, this is a key period in the healing process, RICE to get the swelling down and then get the movement sorted.  I didn't when I was a kid and it now goes over every now and again.  The resulting damage over the years means it naturally sticks out about 30 degrees more than the other.

Badger your doc until he refers you :y
Title: Re: Suspected head gasket failed 3l v6
Post by: elitedave on 14 April 2013, 14:50:58
can real rest that much m8 mrs is mental ill i got do the lot need car two pluss i got a 8 week puppy to deal with

my back is wearing out any way
 i have quit a large thoracic curvature and a compansating lumbar curve


im dosed up on opiates swelling gone right down now not to bad

not the the brightest idea but its a long walk to nearest bus stop

good news is i found out where coolant is pissing out ofthe pipe from coolent bridge to HBV is perished an split

if fixed that

bad news is i drop the dam pelunum and busted the bit that hold spring on throttle cable at throttle body's

and one know if you can weld it or i need a new throttle or another boddge

here
(http://img716.imageshack.us/img716/2194/20130414142237.jpg)
Title: Re: Suspected head gasket failed 3l v6
Post by: dbdb on 14 April 2013, 16:51:01
You can probably drill and tap a bolt thread for it, or I think that plenum is ally unlike the facelifts so could be welded.  However best fix the leak and see if you head gasket is gone or not first.  Good luck. 
Title: Re: Suspected head gasket failed 3l v6
Post by: dbug on 14 April 2013, 17:02:31
Glad you've found the leak mate - as I thought it was the coolant bridge hose :y

Regarding damaged plenum, might be prudent to get replacement off a scrapper.  Possible to "bodge" short term.

By the way all the V6 plenums are ally ???
Title: Re: Suspected head gasket failed 3l v6
Post by: elitedave on 14 April 2013, 17:26:51
thans guys

iv have fixed hose went to start but dident start

but it probably was not enough juice in bat as i only got 3 and a half try`s to it was flat guess the fuel rail needed to pressurize unless i knocked a plug off or something while in there i did lok but can see anything

just got battery on a fast charge so if it dont start after a couple of gos
ill stick the "My Naff Code Reader" and lap top and see if anything trowing up a error

I don't suppose there any one near in or around luton that's got a cheap throttle control body knocking around cheap
by any chance
Title: Re: Suspected head gasket failed 3l v6
Post by: albitz on 14 April 2013, 18:38:41
I might have one.Cant check as Im at work until later.Can check and let you know tomorrow. Definetely got a plenum,just cant remember whether it still has throttle body attached to it. :-\ ;D
Title: Re: Suspected head gasket failed 3l v6
Post by: elitedave on 14 April 2013, 19:20:26
well not losing any water at all ran it for an hour cant drive unless i use some string to throttle body lol

but i aint lost a drop running perfect on about 95degres on temp gage and op com gives same reading

all cylinders are sparking and fire ing no misfire that i can hear

no white smoke bit of condensation out of tail pipe and water drip made me a bit paranoid but aint nothing missing from header tank

never looked before do you get a bit of condensation drip with the omegas

but had a maf fault code but that was lose plugg fixed that

but i got a 59 intake manifold value 1 low voltage fault  and engine manment light on i clear after poking around in engine bay
once fingered that was lose plug or doggy wire was ok for a bit

but come back now its driving me nuts

anyone got a idear

 
Title: Re: Suspected head gasket failed 3l v6
Post by: RobG on 14 April 2013, 19:29:04
well not losing any water at all ran it for an hour cant drive unless i use some string to throttle body lol

but i aint lost a drop running perfect on about 95degres on temp gage and op com gives same reading

all cylinders are sparking and fire ing no misfire that i can hear

no white smoke bit of condensation out of tail pipe and water drip made me a bit paranoid but aint nothing missing from header tank

never looked before do you get a bit of condensation drip with the omegas

but had a maf fault code but that was lose plugg fixed that

but i got a 59 intake manifold value 1 low voltage fault  and engine manment light on i clear after poking around in engine bay
once fingered that was lose plug or doggy wire was ok for a bit

but come back now its driving me nuts

anyone got a idear
That`s 3 times you`ve asked ::) ;D
Title: Re: Suspected head gasket failed 3l v6
Post by: dbug on 14 April 2013, 22:04:12
Rear multiram plug loose/not connected ;)
Title: Re: Suspected head gasket failed 3l v6
Post by: elitedave on 15 April 2013, 20:21:39
yep broken  wire on it

seems promising its running fine  or seems to me cant drive to throttle body's get here temp is spot on at 95 when up to temp no water lose  it for an half an our or so
oil seems fine

no sign of oil in water from what i can see

only thing that is worrying me is i wiped the usual manaze out of filler  cap before running as i like a clean engine and was cleaning up after work

it but was a fare bit back in there later after running at stand still for a while wiped rune again same again but bit less

but everything else seems fine apart from that it possible that that was vapor from all the leaks and it boiling when pump failed clearing it self out
but  does seem a bit odd to me

i am kind of wishing i changed oil cooler while it was in bit
as i got one in cupboard

but i does seem to be running to well for head gasket
just wishing i knew for shaw
any ideas guys
 



Title: Re: Suspected head gasket failed 3l v6
Post by: dbug on 15 April 2013, 20:48:35
Mayo on oil cap on V6 normal for short runs ;)  Nothing to worry about
Title: Re: Suspected head gasket failed 3l v6
Post by: elitedave on 16 April 2013, 09:18:02
well i remembered to re join breakdown insurance no for got and to pay for two from harlow to luton

just seemed a bit more than normal but fingers crossed if it starting to go on head

i will  k-seal it and see what i can get on a trade in
to a deserving stealer if i do ill im thinking about a rover 75 cdti

im hoping to keep it for now fingers crossed

if it ok some time this year im due some case form a insurance pay out

and was thinking may be a s class diesel  few about under 60k for under 5grand
any one got any diy experience on em
Title: Re: Suspected head gasket failed 3l v6
Post by: elitedave on 16 April 2013, 09:26:35
oh one thing i did notice when working on it was

where the bridge from egr to plenum the asked it shot and fell to pieces when removed but it seem to idel ok just put back with out gasket for now

but would that effect anything was thing of just sticking a banking plate
Title: Re: Suspected head gasket failed 3l v6
Post by: dbug on 16 April 2013, 16:19:11
well i remembered to re join breakdown insurance no for got and to pay for two from harlow to luton

just seemed a bit more than normal but fingers crossed if it starting to go on head

i will  k-seal it and see what i can get on a trade in
to a deserving stealer if i do ill im thinking about a rover 75 cdti

im hoping to keep it for now fingers crossed

if it ok some time this year im due some case form a insurance pay out

and was thinking may be a s class diesel  few about under 60k for under 5grand
any one got any diy experience on em

Shouldn't do that mate on an Omega - will cause all sorts of problems in the future ;)
Title: Re: Suspected head gasket failed 3l v6
Post by: elitedave on 16 April 2013, 18:51:44
well news seems to be good
got throttle body at 11am  after a cans of carb cleaner and some  polishing
iv fitted em and been out for a spin

an its smooth and pulling like a train

low down  grunt is better than its ever been and its iderling better that ever

Im wondering now if the vac box on back of plastic muilti ram was all ways duff since i had it all other vac lines and wiring was fine and been checked before.

no sign of wrter in oil marked header tank and been out a few ours in it and it aint lost a drop

could do with a oil change now so ill run a week if all ok ill treat to some of vx oi,l a filter and some new plugs
got a new fuel filter for it as well laying around
 

like to thank everyone for there help with sort and encouragement  to have it all off and look
Title: Re: Suspected head gasket failed 3l v6
Post by: kevinp58 on 16 April 2013, 19:42:44
well i remembered to re join breakdown insurance no for got and to pay for two from harlow to luton

just seemed a bit more than normal but fingers crossed if it starting to go on head

i will  k-seal it and see what i can get on a trade in
to a deserving stealer if i do ill im thinking about a rover 75 cdti

im hoping to keep it for now fingers crossed

if it ok some time this year im due some case form a insurance pay out

and was thinking may be a s class diesel  few about under 60k for under 5grand
any one got any diy experience on em







Absolute crap mate they are like most rovers and suffer from head problems. ::) ::) :-X
Title: Re: Suspected head gasket failed 3l v6
Post by: henryd on 17 April 2013, 15:45:56
well i remembered to re join breakdown insurance no for got and to pay for two from harlow to luton

just seemed a bit more than normal but fingers crossed if it starting to go on head

i will  k-seal it and see what i can get on a trade in
to a deserving stealer if i do ill im thinking about a rover 75 cdti

im hoping to keep it for now fingers crossed

if it ok some time this year im due some case form a insurance pay out

and was thinking may be a s class diesel  few about under 60k for under 5grand
any one got any diy experience on em







Absolute crap mate they are like most rovers and suffer from head problems. ::) ::) :-X

Bmw engine in the 75 diesel :y
Title: Re: Suspected head gasket failed 3l v6
Post by: Marks DTM Calib on 17 April 2013, 15:51:20
Yep, not to many issues with the CDTi in the 75.

The 75 is a bit of a dissapointment for what is supposed to be a large exec car though.
Title: Re: Suspected head gasket failed 3l v6
Post by: elitedave on 17 April 2013, 17:04:42
omega seem fine now so keeping that for now really attached to it lol

if i  do change later it will be a S class diesel   merc with about 40-50 on clock if i can stomach the insurance lol

75 was only option if omega was shot for a bit due to cash at the moment and i much prefer  rear wheel drive

Title: Re: Suspected head gasket failed 3l v6
Post by: symes on 17 April 2013, 18:08:54
K-seal+kill ya miggy